Sliding the headstock easier

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adrianpglover
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Sliding the headstock easier

Post by adrianpglover »

How do I go about getting my headstock to slide easier along the way tubes? I've tried both waxing and rotating the tubes, but I don't see much of any improvement with it. I'll get it to the point where it will slide pretty easily through some of the distance, but then it will hit a section with increased resistance. As far as I can tell there are no nicks or warping in the shape of my way tubes. Just watching some of Michael Young's videos and it takes me quite a bit more to get my setup changed over from one mode to another due to needing to brace myself against the tool to move the headstock.
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DLB
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Re: Sliding the headstock easier

Post by DLB »

This is like Jeopardy, all answers are in the form of questions... I'm just shot-gunning some starting points. The main possibilities here are that the way tubes are not parallel and/or one wedge lock is binding. The idea of rotating a way tube is that there is no perfect tube and you are trying to make the in-tolerance curves parallel. I've never tried to measure this parameter, but one could measure the inside or outside tube spacing to see how parallel they are. I don't know the tolerance, but if your machine is dragging perhaps that would imply one.

Your machine is very new from my perspective, and we are informed that sometime recently the company changed the Bench and Way Tubes material and construction to thin walled stainless steel. I have zero experience with the new tubes, so first question is do you know if your way tubes are thin walled stainless? If you don't know, my first suggestion: move the headstock to one end of the machine and partially raise the other; loosen the two setscrews on the top of the DT Base Arm and remove the Arm. 1) measure the wall thickness, which likely matches a standard sheet metal thickness. 2) Look for the seam on the inside of the tubes, in most cases they would be "clocked" the same as each other and likely in the 6 or 12 o'clock position. (Note - there could be anti-crush inserts in the tube making this more difficult, but as far as I know at present these are only found in the thin walled bench tubes.)

Does the carriage move easily throughout its range? (Test both with the headstock locked and unlocked.)

Does the headstock move more easily if the carriage is unlocked? Does the headstock move more easily if you further loosen its lock (try loosening it to its maximum)?

You might try removing the headstock and waxing the way tube bores. If that helps at all, I would repeat for the carriage.

- David
adrianpglover
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Re: Sliding the headstock easier

Post by adrianpglover »

Thank you for the detailed response. I had not realized that there was a change in the tubes at all, so I'll go check that.

I have rotated the tubes, trying to find the sweet spot. I thought the theory in this was more that the tubes may be straight, but somewhat out of round and you were trying to get the headstock to slide on more rounded part of it.

For the most part, the carriage does slide smoothly, though sometimes with the table on it I have some difficulty. I haven't paid attention to if this is more so from me pushing off center or if it's just getting stuck more easily with the table locked on it.

I've tried unlocking the headstock to maximum, and then sliding the lock forward and back to make sure the wedges are freed up, and this doesn't really change the behavior.

I think I'll check the tube thickness and then reclock them at either 6 or 12 to start over on that part of it.
Mark 7 (new 2020 - pre-COVID) | 12" planer (new 2020 - pre-COVID) | 11" bandsaw | 4" jointer
Grizzly G1023RLWX (new 2013) | Grizzly G0583Z (new 2012) | DeWALT DW618PK
Oneida Dust Deputy (on 5g bucket bolted to a 10g oil drum, used only with planer & jointer)
edma194
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Re: Sliding the headstock easier

Post by edma194 »

adrianpglover wrote: Tue May 20, 2025 7:51 am I thought the theory in this was more that the tubes may be straight, but somewhat out of round and you were trying to get the headstock to slide on more rounded part of it.
I think it's more likely the tubes are not straight and the distance between them at any one point varies. By rotating you are trying to align two curved tubes so the distance between them is more consistent across the length. IOW () is a problem, you want )).
Ed from Rhode Island

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JPG
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Re: Sliding the headstock easier

Post by JPG »

OR (( and not )(. ;)
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DLB
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Re: Sliding the headstock easier

Post by DLB »

adrianpglover wrote: Tue May 20, 2025 7:51 am I've tried unlocking the headstock to maximum, and then sliding the lock forward and back to make sure the wedges are freed up, and this doesn't really change the behavior.
There is variation in wedge lock preset. When I unlock my headstock to maximum, the lock assembly won't move in and out because both wedges are fully retracted (outboard, away from the way tubes) into the housing. The 'other' way to reach 'maximum' is for the front side lock (wedge) to meet the lock handle and act like a jam nut. In that case, the wedges are less retracted allowing the assembly to rattle in and out. Mine will make just over 3-1/2 turns from locked to fully unlocked. That's way more than necessary for normal use, so I'm not suggesting that this is your problem, only that it is a variable to consider.

- David
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