Quill Wobble
Posted: Wed Mar 28, 2007 6:13 pm
I discovered a wobble or side-play in the quill (not the spindle bearings, which are tight) of my lightly used ShopSmith. By wobble/side-play I mean movement when the quill is extended from the housing. There was no wobble when the quill was retracted. The quill side-play was measurable with the quill extended 2". You can measure this side-play using feeler gauges.
The side-play existed mostly in the 3:00 o'clock to 9:00 o'clock (horizontal) plane while looking at the business end of the quill from the tailstock end. The vertical play is restricted by the set screw. I first noticed the side-play when I tried to use the Shopsmith for horizontal boring and I had the quill extended. It would also have been a problem if I had been using it in the drill press mode or with the mortising attachment.
As a note of reference, I purchased my ShopSmith reconditioned at a traveling show, but I have not had much time to use it until recently. The quill shows no wear. None. It looks like new. It still has all of its factory bluing/blackening. The inside of the housing shows no visible wear. The bearings are tight. I measured the diameter of the quill housing (1.742) and the diameter of the quill (1.739). You do need some play for a "sliding fit" or you will cause excess wear in the future.
I only have used the ShopSmith as a drill press twice, so I had not noticed this issue before. I mainly use the ShopSmith as a table saw, sander and twice as a lathe. I have a zero clearance insert, so I do not frequently adjust the blade by moving the quill in and out. I must add that this ShopSmith makes really clean, sharp cuts on oak using the original standard blade.
I looked for answers here and called the 800#. They said to tighten the set screw that impinges the top slot of the quill. That did not stop the side-play. They also said to look at the spline Drive and Ring Assembly. Nothing was worn there. The splines are like new. The also said to tighten the knurled ring. It had no effect on the side-play. My prior phone calls always produced a quick-fix or solution. I like this partnership, but no partnership is perfect.
Here is what I finally did:
I cleaned out the old wax with ethanol alcohol (probably should have used the acetone) and gave it a very very light scuffing with 600 grit wet-dry paper to make sure the glue had something to adhere to.
I secured a piece of .0015 steel shim stock. I superglued it into the side space between the quill and the housing with THICK slow-setting Superglue. I sprayed the shim (after placing it into position) with the acetone spray to set the Superglue. I also had a neoprene glove on my hand to prevent getting my fingers stuck to the Superglue (the glove did get a little stuck, but it released). The quill was not inserted until the glue was really dry.
The size of the shim was about 3/4" x 1". I dry-fitted the shim with the quill inserted. I bent 1/4" of the steel shim outside the housing as a tab to (a) be able to reverse the process, (b) see the position of the shim after the quill was inserted and (c) prevent the shim from traveling back into the housing in the event the glue did not hold. I placed the shim in the inside area between the 9:00 o'clock and 12:00 o'clock position where there is a broad surface and not just at the lip of the housing.
After the glue set up, I gave the shim one more light buffing to remove the excess glue and remove any high spots. I also burnished the surface of the installed shim with the shank of a screwdriver.
The quill was a little tight at first, but after a few strokes, it worked like it should AND there is no wobble with the quill extended. No wobble. Waxed the quill as always.
This repair is reversible.
I credit the Traveling Woodworking Academy for the confidence acquired to go about making this repair/modification.
The side-play existed mostly in the 3:00 o'clock to 9:00 o'clock (horizontal) plane while looking at the business end of the quill from the tailstock end. The vertical play is restricted by the set screw. I first noticed the side-play when I tried to use the Shopsmith for horizontal boring and I had the quill extended. It would also have been a problem if I had been using it in the drill press mode or with the mortising attachment.
As a note of reference, I purchased my ShopSmith reconditioned at a traveling show, but I have not had much time to use it until recently. The quill shows no wear. None. It looks like new. It still has all of its factory bluing/blackening. The inside of the housing shows no visible wear. The bearings are tight. I measured the diameter of the quill housing (1.742) and the diameter of the quill (1.739). You do need some play for a "sliding fit" or you will cause excess wear in the future.
I only have used the ShopSmith as a drill press twice, so I had not noticed this issue before. I mainly use the ShopSmith as a table saw, sander and twice as a lathe. I have a zero clearance insert, so I do not frequently adjust the blade by moving the quill in and out. I must add that this ShopSmith makes really clean, sharp cuts on oak using the original standard blade.
I looked for answers here and called the 800#. They said to tighten the set screw that impinges the top slot of the quill. That did not stop the side-play. They also said to look at the spline Drive and Ring Assembly. Nothing was worn there. The splines are like new. The also said to tighten the knurled ring. It had no effect on the side-play. My prior phone calls always produced a quick-fix or solution. I like this partnership, but no partnership is perfect.
Here is what I finally did:
I cleaned out the old wax with ethanol alcohol (probably should have used the acetone) and gave it a very very light scuffing with 600 grit wet-dry paper to make sure the glue had something to adhere to.
I secured a piece of .0015 steel shim stock. I superglued it into the side space between the quill and the housing with THICK slow-setting Superglue. I sprayed the shim (after placing it into position) with the acetone spray to set the Superglue. I also had a neoprene glove on my hand to prevent getting my fingers stuck to the Superglue (the glove did get a little stuck, but it released). The quill was not inserted until the glue was really dry.
The size of the shim was about 3/4" x 1". I dry-fitted the shim with the quill inserted. I bent 1/4" of the steel shim outside the housing as a tab to (a) be able to reverse the process, (b) see the position of the shim after the quill was inserted and (c) prevent the shim from traveling back into the housing in the event the glue did not hold. I placed the shim in the inside area between the 9:00 o'clock and 12:00 o'clock position where there is a broad surface and not just at the lip of the housing.
After the glue set up, I gave the shim one more light buffing to remove the excess glue and remove any high spots. I also burnished the surface of the installed shim with the shank of a screwdriver.
The quill was a little tight at first, but after a few strokes, it worked like it should AND there is no wobble with the quill extended. No wobble. Waxed the quill as always.
This repair is reversible.
I credit the Traveling Woodworking Academy for the confidence acquired to go about making this repair/modification.