Today in the shop (turning problem)
Posted: Mon May 19, 2014 12:08 am
Here is the situation, I've been working on making some pendants but today I ran in to an issue that has me pretty much stopped in my tracks.
Forward
I purchased a faceplate that has a center hole and a series of "off-center" holes. I have this mounts by way of a 3/8" stud that is mounted in a shopsmith router chuck by way of a 3/8" to 1/2" adapter. That faceplate then has a series of screw holes that allows the secondary plate to be mounted in any of the 24 locations available. Don't worry pictures are coming.
To the secondary plate has screw holes to mount a waste block. Like other projects the waste block becomes the place the project is mounted for turning. So first I true up the block so it runs round and flat. Then I turn the area where the pendent will mount, a smaller area so I can tape the project piece down but still get my fingers in to remove it (held on with double side tape).
As mentioned here are the pictures:
[ATTACH]25069[/ATTACH]
This is the collection of parts.
[ATTACH]25070[/ATTACH]
When assembled it looks like this. Note the "0" and "0" are lined up.
This is where I trued up the block and have it ready to mount the pendant.
[ATTACH]25071[/ATTACH]
This show the front or working face.
[ATTACH]25072[/ATTACH]
The pieces have been rotated 180 degrees.
Problem
This attachment is normal sold with a MT2 to 3/8" drive for use in more conventional lathes. I'm using a cut off bolt which I made to turn bottle stoppers and that sort of thing. It has worked well for that and in fact I have made two of these for convenience. I tried both of them.
In this video things are setup and working pretty much the way it is expected to work.
https://www.youtube.com/watch?v=wFk890juj5k
The lathe is running at 1000 rpm and I would have no problem making a pendant and in fact I have.
In this video the index was changed so it is 180 degrees from the previous setting.
https://www.youtube.com/watch?v=WXkWkZn8BPk
As you can see it is wobble time, this would be very difficult to do any fine turning with it this way.
I stepped back to just the faceplate for this video.
https://www.youtube.com/watch?v=DBD36l-bO5M
Indeed the issues is clearly presenting it self already.
So as of right now the indexing is not functional except at "0" "0".
My problem is which part is causing the issue. It could be the bolt but the faceplate seems to run pretty well on it side edge.... the faceplate could either be drilled a bit off or the face might not be flat.
I plan to contact the seller but I though I give you guys a shot at providing some input. I'm no lathe expert so maybe you will see something amiss.
Worse case I guess I could have an adapter made, 5/8" shopsmith to 3/8" x 16........
Ed
Forward
I purchased a faceplate that has a center hole and a series of "off-center" holes. I have this mounts by way of a 3/8" stud that is mounted in a shopsmith router chuck by way of a 3/8" to 1/2" adapter. That faceplate then has a series of screw holes that allows the secondary plate to be mounted in any of the 24 locations available. Don't worry pictures are coming.
To the secondary plate has screw holes to mount a waste block. Like other projects the waste block becomes the place the project is mounted for turning. So first I true up the block so it runs round and flat. Then I turn the area where the pendent will mount, a smaller area so I can tape the project piece down but still get my fingers in to remove it (held on with double side tape).
As mentioned here are the pictures:
[ATTACH]25069[/ATTACH]
This is the collection of parts.
[ATTACH]25070[/ATTACH]
When assembled it looks like this. Note the "0" and "0" are lined up.
This is where I trued up the block and have it ready to mount the pendant.
[ATTACH]25071[/ATTACH]
This show the front or working face.
[ATTACH]25072[/ATTACH]
The pieces have been rotated 180 degrees.
Problem
This attachment is normal sold with a MT2 to 3/8" drive for use in more conventional lathes. I'm using a cut off bolt which I made to turn bottle stoppers and that sort of thing. It has worked well for that and in fact I have made two of these for convenience. I tried both of them.
In this video things are setup and working pretty much the way it is expected to work.
https://www.youtube.com/watch?v=wFk890juj5k
The lathe is running at 1000 rpm and I would have no problem making a pendant and in fact I have.
In this video the index was changed so it is 180 degrees from the previous setting.
https://www.youtube.com/watch?v=WXkWkZn8BPk
As you can see it is wobble time, this would be very difficult to do any fine turning with it this way.
I stepped back to just the faceplate for this video.
https://www.youtube.com/watch?v=DBD36l-bO5M
Indeed the issues is clearly presenting it self already.
So as of right now the indexing is not functional except at "0" "0".
My problem is which part is causing the issue. It could be the bolt but the faceplate seems to run pretty well on it side edge.... the faceplate could either be drilled a bit off or the face might not be flat.
I plan to contact the seller but I though I give you guys a shot at providing some input. I'm no lathe expert so maybe you will see something amiss.
Worse case I guess I could have an adapter made, 5/8" shopsmith to 3/8" x 16........
Ed